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scott1984

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Posts posted by scott1984

  1. Got an 2008 f350 6.4 with a ford reman. Came in pushing coolant tested both egr cooler found blown head gaskets Pulled cab and pulled both heads found both heads warped. Got the heads fixed put all back together bled the fuel system while cab was off no leaks. Super right nope. Truck cranked up ran good felt good about it. Next day came in to finish it up. Tried to start it and if would hit for a brief second and nothing hooked. Hooked the IDS up and seeing FRP was going over 5000 but I as soon as the key was key was released it shows 124 psi so I figured there must been air in the system bled again and no air. Im thinking the HPFP has gone bad but Im not 100% sure because FRP showing me that it hit for a second. Any help would be great

  2. They are a pain on the LMM transmission has to come out cause of a coolant tube runs directly over the turbo. If its a LBZ still bad but you can get it out just gotta go the pass. side wheel well to get the pipes loose. Need several 12mm 12 point sockets for all the pipes but the down pipe. 

  3. If they aint used he must have put them in without the moly lube they sent and left the hood up. The indy may have priced his self of the job. Personally I love the 6.0 even when they were under warranty. I left the dealer world years ago and still get these things to work on but if had I this job I would send it away

  4. After reading this story. I wouldn't feel bad at other than his pop pass away. The kid should been after the first bolt broke to stop. Its time to learn that mistakes cause money. I don't mind helping people out I'll answer question but don't call me raising hell cause you broke something or did it your way.

  5. Ok as the title says got an 06 ford 350 6.0 with a blowed egr cooler no big deal. Went to bring the truck in the shop and yes it came in on the hook. Hopped in turned the to start postion and it sounded like a car with a broken timing belt. That zing sound. So i pull the glow plugs and checked compress highest i got was 10 psi. So there for I was thinking bent rods right. Pulled heads off to check for piston protusion and dead on spec. Never seen rings cause this issue before. and they does not want a short block.

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