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leon

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Posts posted by leon

  1. "but like my original post, remove the convolute from the clutch coil harness take out and give both wires a good tug. Just to be sure. "  (Keith Browning)

    I did and I did find the ground circuit broke at one of the zip ties,  they were really squeezed tight and I went so far as to go back in the harness as far as I could and cut out the power and ground circuits to my coil, and installed about 7 " good wire performed wiggle test again and all good.  You told me twice, I knew you meant business. Thanks for that.

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  2. True, on that Keith. I cannot tell you how much air was in the system.  I just know that our machine purged air for a long period of time after recovery (much longer than normally experienced).  I recharged a bit less than the spec. just to operate the system to see if pressures went high again.  The pressures were at 225 high side and 36 low side at 93 degrees with 80% humidity in the shop.  the air flow from the center vents was normal and 44 f. I operated it a couple of times with about 30 minutes rest in between. and both times it worked normally.  I appreciate the heads up on the wire issue, and yes there is a message or bulletin on that.  I will open that wiring convolute up and verify the circuits...the wire ties appear to really be tight on the loom.

  3. Keith I have 2 '17s right now both no cold air both a/c compressor not engaging.

    the first one I have a multitude of problems, 1 being the ms CAN is down.  I also load tested the wires from c1046 to the compressor clutch, they were good,  I attempted to power and ground the clutch and it does not engage with my power probe.  I also unplugged all the connectors in the rear of the truck looking for water and corrosion, I did't see anything but for some reason my ms CAN came back and hasn't faultered since.  I wired in a fog light bulb into the compressor connector and it will light when I turn on the ac, I am waiting on a coil/clutch for it.

    #2 f550 low and high sides are super high, evacuated and got 1lb. 12 oz. and a shit ton of air. recharged at 1, 8. and am monitoring the system for operation, it is very cold at center vent 44 degrees.  blower works on all speeds. system seems right.  just not sure why I had air in the system. air flow from vents feels normal at all speeds.

  4. Thanks, Chad.  I think my problem on finding information on this was I was lookling for des.and op. of a level/heater assembly

    For some reason I couldn't grasp the reductant quality module as being my target...  I guess... I suppose its time to revisit the pced

    and enjoy some quality reading.

  5. Ok guys, I was on this same thought path, but I was having a hard time making sure.  It seems to reason to me

    that its most likely the way it is going to operate.  Keith I was looking through that section and...well I didn't see what I was looking for.

    I'm sure you are right.  thanks for the replies

  6. I am trying to find information on the operation of this gauge, customer complains of gauge drops from full to @ half  with no indication in between

    it came in reading @ half and I put in 2 gallons and it is reading full.  No codes in ipc.  I'm not sure what type of level sender it is using,  And I can't

    seem to find what I'm looking for in the wsm or pced. 

  7. I have a truck in here it is a 11 550,  it has multiple problems to diag, but it also had the 16b24.

    I have no excuses for my mental lapse but right now I have a lot of stuff going on here and at home.

    I was trying to be efficient about things and while I was performing a prior approval on a def heater

    for another truck I thought I would at least get the 16b24 done.  About 3/4 of the way through it hit me

    that the dpf had been deleted.  customer just bought this truck 6 months ago in a different state and

    doesn't have the programmer.  Well, I feel like a real idiot right now and short of putting all the ex. components

    back on, (which he doesn't have either), I will probably end up buying a dpf delete programmer.  I have to look

    at costs here so I am asking if anyone has a cost effective programmer or alternative ideas?

  8. keith, thanks, I did see that and what I eventually found was

    at the dlc the boom rig is connected to the dlc and the wiring

    from the upfitting is a little "rough" . found a strand of

    wire sticking out from loom and making connection with another

    the wires were stipped back quite a way and I tried to remove

    and heat shrink over them for the repair but they were too large

    to fit back into the connector...taped the hell out of it, has

    been gone for a while now

  9. 08 f550, u0073 in pcm, I remember reading on a post either

    here or on PTS that some people were finding a wire chafe

    around the radiator area, can someone enlighten me as the

    specifics? Ive checked tbc and rcm wiring, this is an intermittant problem. this has a stellar boom on it and I have

    checked the wiring at dlc for issues and do not see any problems, my arms and hands are tired from wiggling and yanking on harnesses!!!!

  10. ok, I feel compelled to let anyone interested know what fixed this one. first off, late build 04 with a 6speed 4x4,

    at times at start it will run verrry slow (150-300 rpm's)

    when this happens synch pid goes to no

    ficm synch yes, and yes it is still running,

    do not loose cam or crank sensor to pcm

    I swapped both cam and crank sensors with another truck no difference, overlayed wiring from both sensors to pcm again no

    difference, attempted to move crank trigger wheel...no movement

    tried a different pcm and ficm..does anyone see the desperation in this yet? thank goodness for a donor truck that was available

    during this trucks 4week stay. multiple calls to hotline and fse

    visited for one day all of us were still scratching our noggins.

    then...one time while it was doing this I was playing with the

    ignition witch and the starter engaged for a moment while it was

    running, and BAM! it came out of its fit. I was able to do this every time. this truck had a dual mass flywheel and at times on start it would do some sort of crazy resonance shit to the crank and cause it to loose sync a single mass flywheel and clutch fixed it... that should have been my first thought, what a moron!

  11. ok same truck, when this happens it runs on 3-4 cyls, really struggles to keep idling, cannot perform power balance test

    when this happens, also found a very strange pid condition,

    synch pid will read no but ficm synch will read yes, wtf?

    have swapped pcm and ficm and it still occurs, ficm voltages

    are normal when this occurs. this one is starting to get to my

    head!!

  12. I have a 04 f250 that when starting sometimes, the engine rpm's

    slowly go up to idle speed. other times when it stars "normally"

    rps ramp up and then go down to idle speed, (I hope that makes sense). There are no cmdtc's or on demand codes, engine seems to

    run normally and this may happen warm or cold, when monitoring pids found that ipr commanded when this happens is less than 40%

    during crank mode. when it starts normally it goes over 75%.

    monitored ficm synch, rpm, icp, ipr vpwr, vref, and cannot come to any conclusion, changed to 10/30 rotunda still does it, any ideas? this is one I havent seenbefor it has 70k on odometer and looks pretty well taken care of.

  13. this is a ford reman and I assumed responsibility as soon as I

    opened the hood, (powertrain warranty). Have had contact with

    ford hotline and had our fse look at it, we are putting new

    (commonized) heads on as there is no valve train clearance on

    #1 and only .002 on #2, valves are recessed in head about .030

    and pass side engine deck has been machined, not sure how much,

    but will let you guys know what happens, thanks ktmlew for reading this post carefully I know it is difficult to follow.

  14. I am working on a 03 f250, I installed reman long block, as soon

    as I started spinning it over I could tell that there was a

    compression problem with a cyl. found #1 cylinder intake valves

    leaking air, no obvious problems were noticed with valve covers

    off, swapped push rods with another cyl and compression was up

    higher but still 100 psi below others (280 vs 375-390),

    as I was removing cyl head I was running leakdown tester while I

    backed off head bolt and rocker carrier bolts and the air leak

    stopped, comepletely. removed head and replaced lifters on #1 cyl

    reassemble and same thing. the next test was to measure total

    clearance between rocker and crossbar with the lifter collapsed

    of coarse #1 intake had no clearance but others (did all 16)

    ranged from .002 to .040, ok my question is what clearance would

    you be comfortable with? my thinking is that if this was a

    mechanical grind cam that I would need a min of .015 I am looking

    for any input on this sublect. thanks

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