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CISCO

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Everything posted by CISCO

  1. I HAD A 6.4 ABOUT 3 MONTHS AGO THAT WAS LOOSING POWER INTERMITTENTLY AND THERE WAS A PLASTIC BAG IN THE AIR FILTER HOUSING.
  2. 18 F150 1FTFW1E13JFD73922 LOW OIL PRESSURE LIGHT COMES ON VERIFY CUSTOMER CONCERN,PULL CODES NO CODES. ROADTEST 40 MILES OVERNIGHT LIGHT CAME ON 7X.CONTACT HOT LINE ID:1174562. FOLLOW HOT LINE, RECOMMEND ,REMOVE OIL FILTER AND VISUAL INSPECTION FOUND IS MISSING RUBBER NUB AT SPRING PLATE.BUT I FOUND THE RUBBER NUB AROUND THE OIL FILTER HOUSING.ACCEES TO REMOVE OIL FILTER HOUSING AND OIL COOLER REMOVE UPPER INTAKE THROTTLE .REMOVE BOTH SIDE GLOWPLUG .COOLING SYSYTEM BY PASS HOSES AND LEFT VALVE COVER. REPLACE OIL FILTER HOUSING AND COOLER AND ALSO REPLACE OIL PRESSURE SWITCH. REPLACE OIL FILTER AND OIL.REPLACE COOLANT. RETEST OK. ROADTEST OVER NIGHT ,NO MESSAGE AT DASH BOARD LOW OIL PRESSURE. Customer Comment
  3. Replaced the front BPA the front sensor on the master cylinder and its now fixed. Now when I press on the brake pedal both read on and when I release the brake pedal both BPA & BOO read off. Thank you! Hope this helps someone.
  4. I am getting a p0703 Brake Switch B input circuit and when watching the boo & bpa pid only the boo changes states when pressing the brake pedal and bpa stays on all the time. So I went to parts and asked for the brake applied switch and they gave me the sensor that goes on rear of the master cylinder and has three wires going to it and the brake applied switch according to the wiring diagrams is showing only a 2 pin connector, is this right? The 2 pin connector goes to the sensor that goes in the front of the master cylinder which I am thinking its the BPA switch according to wiring diagram. Thank you!
  5. Can somebody please help me I need the part number for the gasket on the high pressure pump reservoir. Thank you
  6. Well the customer texted me yesterday and said that he found the problem and when i asked what it was he said that it was the Dual Mass Flywheel. I never asked him how he found out that it was the Dual Mass Flywheel but it makes perfect sense to me. Thank you all
  7. I swapped ficm & pcm still same thing mostly missing on 2,7,5,&6 at idle only and smooths out as soon as you push on the accelerator pedal slightly. I also disconnected the alternator & also disconnected all injectors 1 by 1 and still same thing. I did notice that when i cancelled cylinder #4 it did not make a difference and as seen on the power balance test. i also performed relative compression test and it passed. Thank you My number is 816-730-2609 you can call me or text me.
  8. Well the customer texted me last night and said the truck was running good and that he did not want to replace the check valves on the high pressure oil rail. Has anybody seen the concern as shown in the power balance test? Thank you
  9. I have an 03 6.0 that misses only at idle and the miss will go away as soon as it comes off idle. The truck runs great and has lots of power but it just misses at idle on different cylinders. ficm voltage 48v icp is good. I know i read somewhere where the check valves on the high pressure oil rails would cause the same problem im having but im not sure. I will be installing the check vavles on the hight pressure oil rails tomorrow morning and will post my results. Thanks in advance
  10. so I took the crossover tube to the high pressure turbo off and checked impeller by hand and it appears to have more than the .89mm radial shaft movement also their is dried gunky oil on the high pressure turbo outlet. so I priced out the turbos I will keep you guys posted.
  11. this truck has an sct tuner 7015 x4 relative compression is good, fuel trims are good except #2 -10, blow-by looks good, this truck feels like I am driving a race car it goes so fast. the truck is consuming oil cause I had to add 5 quarts after drving it for about 60 miles. I quess I thought I was going to see oil coming out of the turbo downpipe but I did not. im leaning towards the turbos. I will keep you guys posted.
  12. I have a 2008 6.4 with 240,000 miles and had engine replaced at 148,000 miles. I have checked turbo inlet, lower cac tube hose, blow-by, and down pipe and I don't see anything. when I removed the down pipe to inspect I only see powdery black soot and it is not wet. Engine has lots of power and will go from 0-90 really quick. Please help thanks in advance.
  13. I STILL DONT UNDERSTAND WHY IT DOES NOT SHOW UP ON THE EBP SENSOR PID.
  14. OKAY CUSTOMER PULLED THE EBP SENSOR & TUBE(LIKE I HAD SUGGESTED IN THE FIRST PLACE) AND THEY WERE PLUGGED UP. CUSTOMER REPLACED EBP SENSOR & TUBE AND IT IS NOW FIXED. THANKS AGAIN.
  15. CUSTOMER BOUGHT A H&S MINI MAXX & TRUCK IS DOING THE EXACT SAME THING AS WITH THE OLD PROGRAMMER. I WILL KEEP YOU GUYS POSTED.
  16. CUSTOMER RETURNED TO STOCK AND DROVE AROUND THE BLOCK AND PROBLEM IS NOW GONE . HE REDOWNLOADED HIS TUNER AND HAS BEEN DRIVING THE TRUCK SINCE SATUDAY(I JUS GOT OFF THE PHONE WITH HIM) WITH NO PROBLEMS .THANK AGAIN
  17. YOU GUYS ARE FUCKING AWESOME! LOVE THE INFORMATION. CUSTOMER IS GOING TO RETURN TO STOCK & THEN RE DOWNLOAD HIS PROGRAMMER AND THEN SEE WHAT HAPPENS. IF IT DOESNT FIX IT I WILL BE LOOKING AT IT SATURDAY. GOOD NIGHT MY AMIGOS. I WILL KEEP YOU GUYS POSTED.
  18. CONT. P2262 P0069 & P006B CUSTOMER SAYS WILL NOT BOOST INTERMITTENTLY UNTIL YOU CYLCE THE KEY AND SOMETHING RESETS AND WILL HAVE BOOST HOT OR COLD. PLEASE LOOK AT PIDS. TRUCK HAS PROGRAMMER. THANKS IN ADVANCE
  19. I HAVE ALSO MIXED THEM UP AND HAVE NOT HAD ANY ISSUES.
  20. I READ ON INTERNATIONAL AUTOMOTIVE TECHNICIAN NETWORK (IATN) THAT IF YOU DRAIN A QUART OF OIL & PUT A QUART OF CLEAN DIESEL FUEL IN THE OIL IT WOULD FREE-UP STICKING FUEL INJECTORS.
  21. I HAVE HAD 2 WATER PUMPS LEAKE AFTER EGR/OIL COOLER REPLACEMENT WHEN USING AIRLIFT TOOL. I THINK THAT IF WATER PUMP IS BORDERLINE, IT WILL FAIL COMPLETELY WHEN USING AIRLIFT TOOL.
  22. JUST WONDERING WHERE TO GO AND HOW MUCH DOES IT COST TO GET A PERSONAL FMC DEALER ACCOUNT. THANX IN ADVANCE.
  23. OKAY TRUCK IS HASNT CAME BACK AND I DO TOO FEEL (AFTER READING REPLIES)THAT IT WAS NORMAL BRAKE PEDAL ACTION. JUST INSTALLED HYDRAULIC CONTROL UNIT IN A 03 6.0 F-450 FOR ABS MOTOR INOP(OPEN CIRUIT CODE). INSTALLED HCU, PUSHED ALL 4 PADS WITH SCREWDRIVER,BLED WITH IDS ABOUT 4 TIMES PEDAL DIDNT SEEM RIGHT SO I MANUALLY BLED TWICE(STILL NOT SURE IF COLLAPSING CALIPER PISTON IS BETTER THAN MANUALLY BLEEDING ALONE),ROAD TEST AND IT WAS PERFECT.
  24. okay found very slight leakage on hcu but lines were tight, so i loosened them and retighten them and re bled every thing again as posted earlier. road test rechecked hcu not leaking but not truly convinced this is the fix. i road tested again,vehicle brakes fine,no safety issue with vehicle not braking and causing an accident. was not trying to pushed on peday like a crazy maniac so i let it go before i read all you guys is post this morning. praying it doesn't come back. i thank all of you for the help i will keep in mind all of the above replies. will be getting some flare plugs as Bruce mentioned sounds like a good idea. will keep you guys posted if it returns,again thanks this is an awsome crowd.
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