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tonybullitt

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Posts posted by tonybullitt

  1. Friend of mine has an early 04 that he says runs good doesn't make any boost. He put a turbo on it made sure the map hose is not plugged still no boost. I told him see if it learns vgt and he said it has now. He took down pipe loose made no difference. Any other ideas I can throw out to a guy with some experience and a snap on scanner? Short of bring it in to me

  2. Here is what I would try. Get a different ids or clear out your ids. Put new pcm in pull fuse id it normal but it won't be able to because fuse is out. It will ask for tear tag and Vin put in then install fuse. Allow it to program it should work fine. It seems the key to programing used modules is a fresh ids. If ids can pull info from a previous session it will even if u tell it not to. I think it pulled the Vin one of the times u id it and has no reason to check because it's the same.

  3. I had a truck at the beginning of the week that had been to a different dealership they gave up on it because it was modified. Then it went to performance shop they tried a new tune in programmer then took it back out. When I got it was programed stock with all egr and egt codes on demand. Had to get customer to bring in programmer and program it to even start looking at it.

  4. I had a truck kick my ass and figured I would share. 2018 start stall went thru PPT leads to fuel pump driver. I jumpered to bypass fuel pump driver truck ran great. Got new driver put in cleared codes went to back out of the stall and it dies. Recheck same codes. PPT leads to driver. Checked like hotline reports guy talked about having to replace driver multiple times to get w good one. So I got one from a no issues truck plugged in. Truck stalled almost immediately. So I print off wiring diagram and see only one connector in-between. When I ohmed the wires they were 3 ohms and that was going they the connector. The connector is above left front tire so I pull the wheel well accessed connector unplugged no issues. I got called away from the truck. When I got back to it the female side of the connector had green water dripping out of the pin in question. Pulled pin out and sure enough corroded right where the pin is crimped to wire. I guess I should have pulled my head out of my ass and load tested the wires when doing PPT. 

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