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RyanG

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Posts posted by RyanG

  1. so anytime you have an upper o-ring coming apart its due to the fact that the oil rail nipple o-ring is shot? I've only come across an upper o-ring coming apart once and I just threw an injector in and shipped it. am I looking at repeat failure down the road?

  2. Its in the 6.7 coolant flush procedure, it says to flush with "fresh water supply" and use hot water if you can, then fill with de-ionized water or distilled water to do the final flush, then drain again and fill with coolant and distilled or de-ionized water. We stock distilled water to fill with coolant also but I don't do the final distilled flush.

  3. One thing I did not see mentioned is water quality with which the coolant is being mixed with. I was told in school that we should always be using distilled or bottled water especially with motorcraft orange and not tap due to the amount of sediment in which caused the scale build up clogging passages. Instructor said that was a huge part of the problem with gm dexcool eating radiators and intake gaskets all through the 90s and early 2000s. I remember doing gm 3100 and 3400 intake gaskets constantly for the leaking gaskets when I was in the aftermarket for repeat leaks.

  4. Yeah the problem as always is educating the customer. Had a 6.4 owner complaining about his oil being overfull all the time saying there was a problem. He changes it every 10k miles because that's what the owners manual recommends. I tried to explain to him about fuel in the oil from regen and dropping the intervals to 5k and so on. He looked at me like I was full of shit and hasn't been back. I think I dodged a bullet.

  5. Had on broken crankshaft, number 5 piston went through side of block, cracked hpfp housing and a few broken rocker arms. same as matt, had to take pictures of pistons hitting heads for long block approval. I was surprised that ford didn't really care about oil change records, truck had 15k but engine hours was closer to 50k. They said as long as the oil filter wasn't original they don't worry about it.

  6. Just got the decline by the customer on one that's been here for 2 weeks. Dead miss on 5, broken rocker arm, removed both valve covers and found every single rocker tip worn down(thought that was pretty impressive). High pressure turbo blowing oil, metal in fuel rails, cracked up pipes. Lack of maintenance, this thing is black inside, oil filter sucked in looks like an hour glass, priced an engine only had 84k on odometer.

  7. We have terrible management right now. All the good technicians are spread so thin right now and nobody that knows what they're doing is applying so they're filling up the shop with an army of dipshits who cause problems like this. We have lost 4 experienced techs over the last 2 years who have left the industry completely and this is what replaces them.

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